Difference between revisions of "Team:Aachen/Lab/Bioreactor/Characterization of Bioreactor"
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=== Final Experiment === | === Final Experiment === | ||
− | The experiment for characterization of the chemostat Bioreactor consisted of a Batch mode followed by the Continuous mode with 3 different dilution rates. We used | + | The experiment for characterization of the chemostat Bioreactor consisted of a Batch mode followed by the Continuous mode with 3 different dilution rates. We used BL21 Gold DE3 pSB1KRDP strain in minimal Carbon medium M9. |
The experiment was designed to keep the dilution rates constant for 3 reactor volumes, so as to obtain constant Optical Density, an indication of the Biomass, within human sampling error, to achieve proof of concept. | The experiment was designed to keep the dilution rates constant for 3 reactor volumes, so as to obtain constant Optical Density, an indication of the Biomass, within human sampling error, to achieve proof of concept. | ||
{{Team:Aachen/Figure|Aachen_Reactor1ODvsD.png|size=large|title = Plot of Optical Density and Dilution versus Time, in hours|subtitle =Chemostat cultivation of in medium M9. We observed stable OD for 3 reactor volumes, with slight variations due to change in the conditions.|size=large}} | {{Team:Aachen/Figure|Aachen_Reactor1ODvsD.png|size=large|title = Plot of Optical Density and Dilution versus Time, in hours|subtitle =Chemostat cultivation of in medium M9. We observed stable OD for 3 reactor volumes, with slight variations due to change in the conditions.|size=large}} | ||
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− | The continuous mode of operation was initiated with a dilution rate of 0.1 h{{sup|-1}} at hour 5. Constant OD was obtained for 9 hours. However, the feed pump was observed to be pumping more medium than the harvest removed by the harvest pump. Hence at our 30, the Master Control Program was modified to change the speed of the harvest pump accordingly. The harvest pump rate was changed to pump 30% faster than the feed pump. The change made is reflected in reduction of OD from an average value | + | The continuous mode of operation was initiated with a dilution rate of 0.1 h{{sup|-1}} at hour 5. Constant OD was obtained for 9 hours. However, the feed pump was observed to be pumping more medium than the harvest removed by the harvest pump. Hence at our 30, the Master Control Program was modified to change the speed of the harvest pump accordingly. The harvest pump rate was changed to pump 30% faster than the feed pump. The change made is reflected in reduction of OD from an average value of 0.78 to 0.76. |
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+ | At hour 48, the first step change in dilution rate was made to 0.3 h{{sup|-1}}. The OD was observed to be stable with few variations within pipetting error. | ||
− | + | A final step increase in dilution rate was carried out at hour 63, where the dilution rate was increased to 0.4 0.3 h{{sup|-1}}. This resulted in OD values for 3 reactor volumes, which lasted for 7.5 hours. | |
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{{Team:Aachen/Footer|color=green}} | {{Team:Aachen/Footer|color=green}} |
Revision as of 20:59, 18 September 2015